(64/364) 2023-02-10_19-21-08.jpg
Glued disk to faceplate - thinning to target to set the play in the mill's transmission's main shaft stack-up
63: Bad DRO - the Axis should be Z and X No way to fix.
62: Junyi - cheng/ shuo\ and Aloon
61: Junyi - cheng/ shuo\ and Aloon
60: Junyi - cheng/ shuo\ and Aloon
59: spindle read head - making blocks to keep epoxy out of the screw-holes
58: Z encoder - made plastic blocks to keep expoxy out of the screw holes.
57: Another project - the handles are too big.
56: Pretty close for an amature
55: Setting bore gauge
54: Top of the spindle - dashed lines show the edge of the wide flat on the oil pan. High places on the left - someone ground them down - but not enough.
65: Read head with teflon wires installed.
66: Printed some tool holders that I mounted on the side of a tool-cabinet. The ones that came with the red ones had slots instead of holes - eveytime I walked by, one would fall on the floor..
67: Read head - Epoxy coated
68: Had to make a special tool to install the Teflon seal
69: Seal installed - The slot to the right is where the sensor head wires will go out.
70: Seal installed.
71: 3D printed tray that fits in the tool cabinet.
72: This was problematic. the bar helped me scoot it into place. But I had to drill the holes on the oil pan one size bigger. I added hardened washers - without the washers it would move out of place as I tightened it. My take is the oil pan should have been matching cast iron and pinned.
73: Can't find trays that are low enough for these drawers.
74: Testing new spindle encoder.